On Sunday we were lucky enough to have some great weather and took our boats out. We took out both of the dinghy we have, both my parent's Vagabond and my Fireball. It was a good day, despite both of the boats needing some repairs that we have been putting off since we last used them. The fireball needed a pintle for the rudder put back on after this trip. The vagabond needed the line that hauls up the centerboard to be fixed. That line had been getting sun burned for some time and on the last trip it finally failed, thankfully both were easy fixes.
Before bolting the pintle back on I put some silicone onto the back of it to ensure that water can't get into the buoyancy chamber at the back. I put way too much on but it is a lot easier to clean up a little silicone before it sets then to repair a rotted out hull.
The vagabond all hooked up and ready to go. To put the new line in the centerboard we had to lift the boat up, drop the centerboard out then run the new line through the hole in it and then put it all back in. Not very long to do thankfully.
This is the lake now. I have never seen it this full before. WE have been very lucky and gotten a lot of rain recently. The ground now has so much water in it that almost as soon as we get significant rain now it starts running off and into the rivers and dams.
For a comparison this is what it looked like before. Where the above photo was taken is further up the bank to the right. Quite a long way up.

Unfortunately I didn't get any photos while we were sailing, but it was a very good day for it and we got some good speed up. Nicole did very well as crew, despite me putting the leeward rail into the water quite a long way a few times.

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On Saturday I finished putting the new gasket that was needed onto the waterpump on my Land Rover. I talked about the beginning of the process here.
The problem I had was that I needed some kind of gasket as a spacer to make sure that the impeller doesn't contact the block as the back of the housing. I decided to have a go at making a gasket out of cork from scratch for the spacer.
Armed with a memory of instructions I found on the internet on how to do this I got started. Getting the outside shaped was amazingly easy. With my ball peen hammer I tapped around the edge of the housing which cut the cork on the corner of the housing.
The rest was a bit more difficult. The bigger open spaces allowed me to use the same hammer technique, however when it got in close to the impeller the hammer couldn't reach anymore so I had to resort to using scissors and checking against the housing regularly.
To get the bolt holes we got 2 hammers, set the ball peen of one over the hole and tapped. This cut the cork or at least made a mark, enough so that I could cut the rest of the hole out with scissors.
You can just see the pump in place. I probably should have painted the fan shroud while I had it out, but I didn't really have the abrasives to clean it up enough for good painting.
In the middle you can see a temperature gauge reading about 80 Degrees Celsius. This was after driving around a bit and seeing how the brakes go and so on. Because the fan is always going it probably takes a little longer to warm up than I am used to with a more modern car, but it still gets there no worries so no concerns there.
Now sitting in the back of the yard so I could get the fireball dinghy out. It will move under it's own power, but only in low range. in high range there seems to be something holding it back. I know the brakes need some work so that is my current theory, one of the wheels might not be letting go properly. After that issue is fixed it should be driving well, just needs a full fluid change then I can get on to making sure it will pass rego.

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While I've got the front of the engine bay apart for replacing the water pump here I have the battery sitting on my back veranda not doing much. So I figured I would give it a charge. However I don't have a proper battery charger. I do have a more sophisticated tool that will charge a battery though.
Enter the laboratory power supply. This one is a fairly cheap one that I picked up off ebay a couple of years ago. It's noting to write home about but it is more than enough for this job. The reason it will work for this is that I can set it to output a maximum of 13.8V which is the standard charging voltage for lead acid batteries. It also has a constant current mode which would be useful for smaller batteries which should be charged slower, but a big one like this can probably handle as much as this relatively small supply will provide.

I just used a set of jumper leads to connect the battery as they are all that I have that will fit the posts built into the battery.

Here we are after about 1/2 to 3/4 of an hour. The battery is still accepting .52A of current into it at the full charging voltage of 13.8V which means that it is essentially full. Certainly close enough for me. Tomorrow or the day after I am going to pull the 2nd battery out of the Land Rover and see if it will charge up. The previous owner said that it didn't charge for him but I want to see exactly what happens as sometimes a "dead" lead acid battery can be brought back to life.

I will leave this battery on charge until I go to bed tonight to trickle it up as much as it will, then I will take it off the charge to reduce the risk of something going wrong, boiling, hydrogen production, etc.

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I've made a start on what needs to be done on my new Land Rover. The biggest thing that had to be done first was replace the water pump. The one that was on it had failed so badly that the weep hole in the housing has a stream coming out of it, even when the engine isn't running. I want to get this fixed so I can keep the engine full of coolant and be able to just start it when I need to move it, rather than having to top it off and then try and do everything as quickly as possible.

This is the new pump. I ordered it from E-Bay. It is still raw metal though so I grabbed a can of Kill-Rust paint that I had sitting around and made it not raw metal.
Looks pretty good. I think I will start doing this to all of the parts I take off, to help protect them and also to make the engine bay look a bit cleaner.

We thought it would be easiest to remove the radiator entirely. I forgot to take a picture, but here it is without a rad. There was about 12 bolts with nuts holding it on so we had to take off the grill and then with 2 of us remove all of them, making sure that it didn't fall down as we undid the last few bolts.

Here is the fan and pulley removed. There is a light coat of rust on the inside of the pulley caused by the leak from the pump. Interesting to note the blade and hole spacing is not even. 2 sides are longer and 2 are shorter. Weird.

Really good access now the radiator is out of the way. The water pump is front and center, ready to be removed.

And now it's gone. It is a little crusty inside the housing, however noting is loose so I'm not going to worry about cleaning it other than the gasket surfaces.

The new pump didn't come with a gasket so I was going to have to work something else out. To get this finished that night we were going to try this to seal it up, which should have worked. However the impeller is so deep that without the thickness of the gasket then it collides with the block and can't spin. So I am going to have a crack at making a gasket for this as a spacer as much as anything and then I should be able to start driving this around the yard.

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